Home Forum Ask A Member 1972 85 hp V4 overheated…..

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  • #217519
    fleetwin
    Participant

      US Member

      The thermostat on this engine is relatively easy to get at. But, you may have to move the ignition bracket. The screws never seem to get seized into that plastic housing.. Although the “vernatherm” inside usually fails open…
      OK, my mistake, the overheat occurred at low speeds, which would explain why the engine didn’t seize and paint isn’t burnt.
      Am guessing you shut the engine down when the horn went off and waited for it to cool. Did you remove the engine cover, did it seem overheated?
      The plastic bag/weeds theory is still a possibility…
      I’m assuming the engine didn’t overheat again when you restarted it…

      #217535
      jeff-register
      Participant

        US Member

        Thanks Don,
        Didn’t know about the relief valves,
        Jeff

        #217548
        amuller
        Participant

          This discussion seems rather inconclusive. Will try to run through the sequence of events.

          Motor is stock except for addition of cooling water telltale.

          Had motor out for the first time since I went through it and ran for about an hour at varying speeds but only momentary full throttle.

          (With the fixed idle and main jets there is not a lot to adjust other than the relationship of timer base position to throttle plates….)

          Motor ran very well to my way of thinking.

          Returned to ramp in 3-4 ft depth (shoaling to 2-3) at around 1500 rpm (no wake area).

          Motor began to slow, looked and saw no telltale discharge, advancing throttle did not produce speed increase, motor stopped and we returned to ramp using trolling motor.

          A few hours later, pulled plugs, checked compression as reported, ran on muffs with no apparent problems. Pumping normally.

          So, do I assume something like the bag scenario and try another run, or dig further into motor first? Drop gearcase? Open thermostat box? Change stat?

          #217552
          billw
          Participant

            US Member

            Well the way that is worded, I would swear you ran aground…….

            Long live American manufacturing!

            1 user thanked author for this post.
            #217553
            Bob Wight
            Participant

              US Member

              Based on no observed tell-tale discharge when the motor slowed down, but pump seemed to be working normally later on the muffs, I’d say you momentarily sucked up a plastic bag or some weeds. I recently had a similar experience when I sucked up some weeds while maneuvering around the dock area. Noticed temp gauge climbing so shut it down before hot alarm went off. I’d take it back out for another run and see what happens.

              Bob

              1937 Champion D2C Deluxe Lite Twin
              1954 Johnson CD-11
              1955 Johnson QD-16
              1957 Evinrude Fastwin 18
              1957 Evinrude 3022
              1958 Johnson QD-19
              1958 Johnson FD-12
              1959 Johnson QD-20

              “Every 20 minute job is only a broken bolt away from a 3-day project.”
              "Every time you remove a broken or seized bolt an angel gets his wings."

              1 user thanked author for this post.
              #217565
              amuller
              Participant

                “Well the way that is worded, I would swear you ran aground…….”

                Think I have to agree. Not hard around but in some mud and maybe picking up something that blocked the intake. Live and learn. Will try another run.

                Alan

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