Home › Forum › Ask A Member › 1955 big twin – bottom plug fouling
- This topic has 15 replies, 5 voices, and was last updated 10 months ago by fleetwin.
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July 19, 2023 at 9:50 am #278262
Those inexpensive inline neon spark testers are a handy tool as well. Just be careful not to accidentally ground one of the connections. Doing this when the sun sets makes the tester easier to monitor as well.
July 19, 2023 at 12:02 pm #278272you never know if condensers are good unless teste dat HV for internal leaks
visit the western region AOMCI magazine articles by Mr.Mohat on testing condensers
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July 19, 2023 at 10:45 pm #278286If you go back to original points & coils please use a burnishing tool on the points. It’s an electrical tool, looks like a fat pen with extra strips of burnishing strips in the top. What it is used for is adding material to the contacts of the points, actually deposits metal material on to the contacts. Originally designed for relays in the 1960’s. Look in mail order electronics supply houses on line please,
Jeff
July 24, 2023 at 12:13 pm #278455UPDATE
I did a thorough inspection of my ignition system Friday to find out what my problem might be.
The coils, spark plugs and everything ese looked fine and tested out with the multimeter as they should.
I also cleaned out the bleeder valve assembly.
Put everything back together and tested it in the tank…..still running poorly. So my next step was to start going through the carb.
I immediately discovered my high-speed packing nut was extremely loose and the high speed needle was as well. I snugged up the nut and adjusted the needle 1/2 turn out from seated and it started right up. It still smoked like a chimney from all the previous fuel loading but the longer I ran it at higher RPM the better it performed.
My conclusion is that it was simply being flooded with an over-rich mixture while at full throttle. I think I may have also had some stale fuel in the carb that didn’t help matters. The bottom plug was being fouled by excess fuel IMHO.
I took it to the lake the following morning (not a casual task in that the lake is over an hour away – which is a long way to drive back if it fails to run on the water). And it started and ran great! I achieved 4200 rpm which is about as good as this motor has ever run.
So for now…. problem solved.
thanks again for all the responses.
July 24, 2023 at 12:24 pm #278456Great feedback thanks for update.
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July 24, 2023 at 4:07 pm #278460Cool!
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